I'm Starting this article thread on behalf of KimiG to help out anyone interested on the forum.
Kimi bought my old set-up of cam's but asked my help to resolve a few Issues with his SX, The car was bought modified and does have a few issues like extremely high fuel consumption,bad idle and low power making only 90RWKW, I stand to be corrected but the car has had a few tunning place try and correct the issues with very limited
I have looked over the car and it does have some nice Items but also a few items that make me scratch my head asking myself what the previous owner and tunning shop was thinking.
Modifications include:
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T28 (Off black top SR)
Cam's (My old set)
63mm Exhaust System
Cone Filter
Adjustable FPR
2 Inline pumps
![200SX_confused1 [smilie=200sx_confused1.gif]](./images/smilies/200SX_confused1.gif)
Water\Meth
![200SX_confused1 [smilie=200sx_confused1.gif]](./images/smilies/200SX_confused1.gif)
Uni-Chip
![200SX_shit [smilie=200sx_shit.gif]](./images/smilies/200SX_shit.gif)
The Start
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I arrived on Saturday and we started stripping the motor to install the new cams after a few minutes of stripping it was found that the intake pipes where filled with oil after installing the new cams we needed a few parts from Midas and with it being so later we called it a day and started on sunday once the cams where installed and all the piping,Turbo and intake cleaned, We could get down to finding the faults and issues.
Faults
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The faults I have found are the engine mounts are shot so me and kimi will source replacements in the future.
The Car also seems to be fitted with two Fuel pumps the stock internal and a Inline pump, I can figure out why this was done but we will tackle this issue once we get there.
There is also Two FPRs on the car the stock Item plus a after market Item plumb into behind it, This is just messy and lazy work by who ever tried to tune the car, I have made a work around by drilling out my spare Stock FPR so we can use the single adjustable item we will swap it in at a later date.
Issues
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Also before stripping the motor it was noted that the timing was very advanced, I not sure why this was done but its thought to be because of the Water\meth system, I personally don't think it was the correct way to this
The Fuel pressure on this motor also seems to be sky high at around 4 bar at Idle with vacuum if the fuel pressure is brought down the car goes into a very lean state just off idle causing the car to splutter this could be caused by a number of things but I personally think it related to the horrible Unichip strapped to the ECU
Maus also seems to have plugged the boost controller (bleeder valve) into vacuum system and vent the un-needed air to atmosphere causing the car to sputter on idle.
The last issue seems to be the excel blow-off valve, This is causing the cars Idle to dip dangerously low to stall when releasing the throttle also the BOV is wide open on idle causing the idle to be un-metered
Future
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We are planning on upgrading the Stock Side mount IC to a FMIC , also we will be upgrading the stock MAF to a Z32 unit plus 440cc injectors and remove the horrible Uni-chip and replace it with a nistune system that I will set-up to help the car run better.
We might even remove the fuel pumps and replace them with a single walbro.
So far Kimi is happy with the little changes I have made but we need to resolve a few issues to bring the car back to it 0.9 boost level and see if We will be keeping the water/meth set-up.
Anyway if anyone is looking for a CA18DE intake cam talk to Kimi he has one for sale.